svana
Jetboaters Lieutenant
- Messages
- 433
- Reaction score
- 400
- Points
- 157
- Location
- Riverview, FL
- Boat Make
- Yamaha
- Year
- 2008
- Boat Model
- SX
- Boat Length
- 23
Well, outing #3 in the new (to me) boat under my belt - had one hell of a day today. I figure I’ll share the whole series of events in case someone picks up on something that I didn’t.
We set out to Egmont Key this morning after me installing a new transom scupper (48h after using 5200 quick set) and patching an open transducer screw hole (24h after using marine tex) earlier this week after noticing that the bilge was running every few minutes last week.
The ride out had no problems, but once we got to Egmont the waves were crashing pretty badly and it “lightly” beached the boat parallel to the shore when the anchor didn’t set. I pulled the boat back out and we reset the anchor about 100’ off shore and just hung out on the boat for a few hours. Come time to leave the boat started no problem and we decided to take a trip around the island before heading back, around 8500rpm. About 15-20min into the ride the port engine took a nose dive, we heard a high pitched whine, it dropped down to around 1500rpm briefly before dying and flashing (what I believe is) the hot oil temp light (middle of the 3 lights - 08 SX230 HO for reference, with the MR-1’s).
I checked the oil level and it was fine, checked the clean out plugs, they were both properly seated and there was nothing felt along the shafts. I didn’t dive in to check from the nozzle side. I of course didn’t have a set of vice grips to clamp the engine and limp in on one, so I gave the engine time to cool down and started it back up. I coasted closer to around 7800rpm going 28mph without any issues when after about 2-3 miles I all of a sudden started to feel us get real sluggish. Figured it was because we were going across some wakes/waves, gave it a little more gas, then realized the swim deck was completely under water. We opened up the engine bay and there was water up to the carpeted walls, about 10-12” deep. The clean out plugs were still properly seated, but the tubes were filled with water.
For reference, the bilge has been on since we left the marina. Obviously it was running non-stop at this point, and luckily it was able to outrun the flood. We were stopped for about 30 minutes while letting the bilge do its thing and didn’t sense additional water entering the boat. At this point we started the engines back up no problem and moseyed the remaining 5 or so miles back to the marina trying to keep the same pace to maintain plane. When we got to the no wake zone we recognized that the engine bay was still flooding but slowly draining as we got back in. We docked right before the marina was gonna close so I couldn’t do anything about it tonight, but will likely be going back tomorrow morning to start assessing the situation. Any recommendations on where to start or what to look for would be greatly appreciated. I’m thinking rinse off the engine bay for sure (avoiding direct contact with the electronics), checking the air filter and oil to make sure they’re dry - it doesn’t look like the water reached that high, or else they likely wouldn’t have started, correct? Target #1 is to source the leak/failure of course.
We set out to Egmont Key this morning after me installing a new transom scupper (48h after using 5200 quick set) and patching an open transducer screw hole (24h after using marine tex) earlier this week after noticing that the bilge was running every few minutes last week.
The ride out had no problems, but once we got to Egmont the waves were crashing pretty badly and it “lightly” beached the boat parallel to the shore when the anchor didn’t set. I pulled the boat back out and we reset the anchor about 100’ off shore and just hung out on the boat for a few hours. Come time to leave the boat started no problem and we decided to take a trip around the island before heading back, around 8500rpm. About 15-20min into the ride the port engine took a nose dive, we heard a high pitched whine, it dropped down to around 1500rpm briefly before dying and flashing (what I believe is) the hot oil temp light (middle of the 3 lights - 08 SX230 HO for reference, with the MR-1’s).
I checked the oil level and it was fine, checked the clean out plugs, they were both properly seated and there was nothing felt along the shafts. I didn’t dive in to check from the nozzle side. I of course didn’t have a set of vice grips to clamp the engine and limp in on one, so I gave the engine time to cool down and started it back up. I coasted closer to around 7800rpm going 28mph without any issues when after about 2-3 miles I all of a sudden started to feel us get real sluggish. Figured it was because we were going across some wakes/waves, gave it a little more gas, then realized the swim deck was completely under water. We opened up the engine bay and there was water up to the carpeted walls, about 10-12” deep. The clean out plugs were still properly seated, but the tubes were filled with water.
For reference, the bilge has been on since we left the marina. Obviously it was running non-stop at this point, and luckily it was able to outrun the flood. We were stopped for about 30 minutes while letting the bilge do its thing and didn’t sense additional water entering the boat. At this point we started the engines back up no problem and moseyed the remaining 5 or so miles back to the marina trying to keep the same pace to maintain plane. When we got to the no wake zone we recognized that the engine bay was still flooding but slowly draining as we got back in. We docked right before the marina was gonna close so I couldn’t do anything about it tonight, but will likely be going back tomorrow morning to start assessing the situation. Any recommendations on where to start or what to look for would be greatly appreciated. I’m thinking rinse off the engine bay for sure (avoiding direct contact with the electronics), checking the air filter and oil to make sure they’re dry - it doesn’t look like the water reached that high, or else they likely wouldn’t have started, correct? Target #1 is to source the leak/failure of course.